The engine machine work is one of the few things you really can't do in a garage, especially on this motor. It was a mess, I replaced the crank, had the engine re-sleeved, had major welding done on both the head and the block due to water jacket rust and corrosion. The shop put in 20 hours of labor just on the head. The entire bill for machine work and parts was something like $5600. $2500 parts and the rest labor.
The block on this car was in reasonable shape but the engine had been bored two or three times so I had to put in new sleeves. I got bought them from LA sleeve. I had the shop install the sleeves and bore them out to standard. I got new standard size AE pistons, and had a replacement crank from another 3.8 Liter engine ground .010 under on the mains and rods. The crank was balanced as were the rods and pistons statically before assembly. The shop put in the freeze plugs, but I did the block paint and the rest of the bock prep myself. I used glyptol where I could, and put new copper washers on all the oil galley bolts. I installed the new head bolts and torqued them down using the 2 bolt technique.
I installed a new distributor drive gear, and oil pump next. Its important when working with any of the bearing cap bolts to have a good quality torque wrench and torque down the main bolts to the correct setting. I installed new Woodrift keys and put the gears on the crank next. Things come together pretty quickly if you have all the parts you need up front. I shot oil into the pump and galleys as much as possible to help get the prime up on the pump. One mistake I made at this point is not getting the distributor shaft aligned to be at the right angle when the engine is at top dead center on number six piston. This mistake cost me some time and a oil pan gasket.
The New oil pump was from a later 4.2 liter Jaguar engine and has a larger displacement than many of the original pumps. It required a custom adapter to be added to the oil pickup pipe shown here. I used new tab washers all around when putting these parts in. the last thing I need is something coming apart in the oil pan!
I'm just about ready to put on the oil pan now, I just need to clean up the mating surface and put down some gasket dressing. The engine shop didn't use glyptol in the crank case, even though I asked for it, but otherwise did a good job. They had the oil pan on the motor when I picked it up so I didn't notice it until I got home. Not the end of the world I guess, since it didn't have it from the factory.
The next step is getting the timing chains in. I started off by getting the lower timing chain tensioners in and torqued down. Then put the upper chain assembly together!
Here is the oil pan all glyptoled up and ready to install.
The timing chain gear assembly was a bit of a challenge to figure out but nothing a little reading in the shop manual couldn't solve. Its really quite a complex setup for its day! Most car engines in this era wouldn't have something like this. Notice the new chain tensioners on the right side. All of the timing chain parts are relatively inexpensive. About $200 for everything.
I'm ready go put the timing chain cover on now. I used Red lock tight and new lock washers on everything that didn't have lock tabs.
One more shot of the timing chain area. I need to get the head ready to install next.
Here is the head back from the shop. This puppy was a major mess. I didn't take any pictures of the water jacket before and after, but it was corroded to a point where most people would have tossed it. Of course it had the correct matching numbers so I didn't want to do this, so the engine shop had to do some major work on it. They cut a hole in the deck and welded up an area where the water jacket had corroded into the intake. Welded all the water ports. Pulled .030 of warp out of the head in 4 stages. Replaced the seats, valve guides, bucket guides, buckets, springs and valves. Decked off .010. They did a cc check and found 102 CC per cylinder, They did pressure test on the completed head and it all checked out. APM put in 20 hours of labor on a head is about 15 more than they usually take, This head had 5 hours of welding alone. I'm buffing out the front.
After the head was buffed out I cleaned it with grease and wax remover and shot the gold paint.
I used one of the Cometic head gaskets which was .051 thick based on calculations done by the shop. The calculation is based on .025 total cut from the head and .020 skim off the block. The shop had to first weld the block up around the water ports where it had rusted, The rust pits were about .050 deep. After welding up the ports they Skimmed .010. A previous rebuild had removed .010 so the total became -.020 plus the -.025 skim on the head for a whopping total of .045. The Cometic gasket is made of a composite material with steel embedded. Unlike steel gaskets it compresses some under load. The .051 gasket should compress down to about .045 with 54 foot pounds of torque theoretically. In this picture you can see the gasket just before the head went on. I used aircraft grade permatex gasket dressing on all the engine gaskets.
The head went on without issue, The next step was setting up the timing. The cams had been positioned to be exactly in the correct position when the caps cam caps were torqued. You can see the notch in the cam exactly in the center. of the front bearing cap. The engine is exactly in the top dead center position and the cam chain mounting disks must be popped out of the gear to line up the bolt holes. To do this, pop the gear onto the cam and tap it back with a brass drift until it is full on the cam, then pop the wire keeper off the front and pull the center out of the gear. Rotate the center until it lines up with the bolt holes and pop it back into the toothed gear. This is hard to understand unless you are doing it but is a really important thing to get right, and difficult to figure out unless you've done it. Once the center is back in the gear and bolted up put the wire keeper back in and put safety wire on the bolts.
Here you can see the the timing chain gear bolts properly setup and the timing chain tensioner. You'll need a special tool to tighten the timing chain. I was fortunate enough to be able to borrow one! Thanks Dick! I have the flywheel and water pump on, but just have the water pump pulley stuck on for fit testing. I also bolted up the motor mounts and oil filter housing.
Here is a shot just before I put on the external oil pipe. I am putting new copper washers everywhere and topping those off with some gasket sealer for good measure. After the oil pipes I'll put the valve covers and torque them down. That is about it for this page. I will continue the rest of the motor construction on the next installment